diff mbox series

[v4] backlight: ktd253: Stabilize backlight

Message ID 20210715113636.1139465-1-linus.walleij@linaro.org
State Accepted
Commit daa37361518bf2d1f591bbdaa7c68b2a43d7af48
Headers show
Series [v4] backlight: ktd253: Stabilize backlight | expand

Commit Message

Linus Walleij July 15, 2021, 11:36 a.m. UTC
Remove interrupt disablement during backlight setting. It is
way to dangerous and makes platforms instable by having it
miss vblank IRQs leading to the graphics derailing.

The code is using ndelay() which is not available on
platforms such as ARM and will result in 32 * udelay(1)
which is substantial.

Add some code to detect if an interrupt occurs during the
tight loop and in that case just redo it from the top.

Fixes: 5317f37e48b9 ("backlight: Add Kinetic KTD253 backlight driver")
Cc: Stephan Gerhold <stephan@gerhold.net>
Reported-by: newbyte@disroot.org
Reviewed-by: Daniel Thompson <daniel.thompson@linaro.org>

Signed-off-by: Linus Walleij <linus.walleij@linaro.org>

---
ChangeLog v3->v4:
- Collect Daniel's Reviewed-by.
ChangeLog v2->v3:
- Read my own patch and realized a bug: when we get a timeout
  we bounce back to max period, but still count down the pwm
  with one leading to an off-by-one error. Fix it by extending
  some else clauses.
ChangeLog v1->v2:
- Alter the dimming code to check for how many ns the pulse
  is low, and if it gets to ~100 us then redo from start.
  This is to account for the advent that an IRQ arrives while
  setting backlight and hits the low pulse making it way
  too long.
---
 drivers/video/backlight/ktd253-backlight.c | 75 ++++++++++++++++------
 1 file changed, 55 insertions(+), 20 deletions(-)

-- 
2.31.1

Comments

Lee Jones July 21, 2021, 2:37 p.m. UTC | #1
On Thu, 15 Jul 2021, Linus Walleij wrote:

> Remove interrupt disablement during backlight setting. It is

> way to dangerous and makes platforms instable by having it

> miss vblank IRQs leading to the graphics derailing.

> 

> The code is using ndelay() which is not available on

> platforms such as ARM and will result in 32 * udelay(1)

> which is substantial.

> 

> Add some code to detect if an interrupt occurs during the

> tight loop and in that case just redo it from the top.

> 

> Fixes: 5317f37e48b9 ("backlight: Add Kinetic KTD253 backlight driver")

> Cc: Stephan Gerhold <stephan@gerhold.net>

> Reported-by: newbyte@disroot.org

> Reviewed-by: Daniel Thompson <daniel.thompson@linaro.org>

> Signed-off-by: Linus Walleij <linus.walleij@linaro.org>

> ---

> ChangeLog v3->v4:

> - Collect Daniel's Reviewed-by.

> ChangeLog v2->v3:

> - Read my own patch and realized a bug: when we get a timeout

>   we bounce back to max period, but still count down the pwm

>   with one leading to an off-by-one error. Fix it by extending

>   some else clauses.

> ChangeLog v1->v2:

> - Alter the dimming code to check for how many ns the pulse

>   is low, and if it gets to ~100 us then redo from start.

>   This is to account for the advent that an IRQ arrives while

>   setting backlight and hits the low pulse making it way

>   too long.

> ---

>  drivers/video/backlight/ktd253-backlight.c | 75 ++++++++++++++++------

>  1 file changed, 55 insertions(+), 20 deletions(-)


Slight change of plan.

Looks like this fixes issues introduced in v5.9.  I tend to only
submit -fixes for issues added during the same merge cycle.

How loudly will you shout if I submit this for v5.15-rc1?

-- 
Lee Jones [李琼斯]
Senior Technical Lead - Developer Services
Linaro.org │ Open source software for Arm SoCs
Follow Linaro: Facebook | Twitter | Blog
Linus Walleij July 21, 2021, 3:25 p.m. UTC | #2
On Wed, Jul 21, 2021 at 4:37 PM Lee Jones <lee.jones@linaro.org> wrote:

> How loudly will you shout if I submit this for v5.15-rc1?


It's cool, the users (PostmarketOS) have the patch applied externally anyway.

Yours,
Linus Walleij
Lee Jones July 21, 2021, 4:28 p.m. UTC | #3
On Thu, 15 Jul 2021, Linus Walleij wrote:

> Remove interrupt disablement during backlight setting. It is

> way to dangerous and makes platforms instable by having it

> miss vblank IRQs leading to the graphics derailing.

> 

> The code is using ndelay() which is not available on

> platforms such as ARM and will result in 32 * udelay(1)

> which is substantial.

> 

> Add some code to detect if an interrupt occurs during the

> tight loop and in that case just redo it from the top.

> 

> Fixes: 5317f37e48b9 ("backlight: Add Kinetic KTD253 backlight driver")

> Cc: Stephan Gerhold <stephan@gerhold.net>

> Reported-by: newbyte@disroot.org

> Reviewed-by: Daniel Thompson <daniel.thompson@linaro.org>

> Signed-off-by: Linus Walleij <linus.walleij@linaro.org>

> ---

> ChangeLog v3->v4:

> - Collect Daniel's Reviewed-by.

> ChangeLog v2->v3:

> - Read my own patch and realized a bug: when we get a timeout

>   we bounce back to max period, but still count down the pwm

>   with one leading to an off-by-one error. Fix it by extending

>   some else clauses.

> ChangeLog v1->v2:

> - Alter the dimming code to check for how many ns the pulse

>   is low, and if it gets to ~100 us then redo from start.

>   This is to account for the advent that an IRQ arrives while

>   setting backlight and hits the low pulse making it way

>   too long.

> ---

>  drivers/video/backlight/ktd253-backlight.c | 75 ++++++++++++++++------

>  1 file changed, 55 insertions(+), 20 deletions(-)


Applied, thanks.

-- 
Lee Jones [李琼斯]
Senior Technical Lead - Developer Services
Linaro.org │ Open source software for Arm SoCs
Follow Linaro: Facebook | Twitter | Blog
diff mbox series

Patch

diff --git a/drivers/video/backlight/ktd253-backlight.c b/drivers/video/backlight/ktd253-backlight.c
index a7df5bcca9da..37aa5a669530 100644
--- a/drivers/video/backlight/ktd253-backlight.c
+++ b/drivers/video/backlight/ktd253-backlight.c
@@ -25,6 +25,7 @@ 
 
 #define KTD253_T_LOW_NS (200 + 10) /* Additional 10ns as safety factor */
 #define KTD253_T_HIGH_NS (200 + 10) /* Additional 10ns as safety factor */
+#define KTD253_T_OFF_CRIT_NS 100000 /* 100 us, now it doesn't look good */
 #define KTD253_T_OFF_MS 3
 
 struct ktd253_backlight {
@@ -34,13 +35,50 @@  struct ktd253_backlight {
 	u16 ratio;
 };
 
+static void ktd253_backlight_set_max_ratio(struct ktd253_backlight *ktd253)
+{
+	gpiod_set_value_cansleep(ktd253->gpiod, 1);
+	ndelay(KTD253_T_HIGH_NS);
+	/* We always fall back to this when we power on */
+}
+
+static int ktd253_backlight_stepdown(struct ktd253_backlight *ktd253)
+{
+	/*
+	 * These GPIO operations absolutely can NOT sleep so no _cansleep
+	 * suffixes, and no using GPIO expanders on slow buses for this!
+	 *
+	 * The maximum number of cycles of the loop is 32  so the time taken
+	 * should nominally be:
+	 * (T_LOW_NS + T_HIGH_NS + loop_time) * 32
+	 *
+	 * Architectures do not always support ndelay() and we will get a few us
+	 * instead. If we get to a critical time limit an interrupt has likely
+	 * occured in the low part of the loop and we need to restart from the
+	 * top so we have the backlight in a known state.
+	 */
+	u64 ns;
+
+	ns = ktime_get_ns();
+	gpiod_set_value(ktd253->gpiod, 0);
+	ndelay(KTD253_T_LOW_NS);
+	gpiod_set_value(ktd253->gpiod, 1);
+	ns = ktime_get_ns() - ns;
+	if (ns >= KTD253_T_OFF_CRIT_NS) {
+		dev_err(ktd253->dev, "PCM on backlight took too long (%llu ns)\n", ns);
+		return -EAGAIN;
+	}
+	ndelay(KTD253_T_HIGH_NS);
+	return 0;
+}
+
 static int ktd253_backlight_update_status(struct backlight_device *bl)
 {
 	struct ktd253_backlight *ktd253 = bl_get_data(bl);
 	int brightness = backlight_get_brightness(bl);
 	u16 target_ratio;
 	u16 current_ratio = ktd253->ratio;
-	unsigned long flags;
+	int ret;
 
 	dev_dbg(ktd253->dev, "new brightness/ratio: %d/32\n", brightness);
 
@@ -62,37 +100,34 @@  static int ktd253_backlight_update_status(struct backlight_device *bl)
 	}
 
 	if (current_ratio == 0) {
-		gpiod_set_value_cansleep(ktd253->gpiod, 1);
-		ndelay(KTD253_T_HIGH_NS);
-		/* We always fall back to this when we power on */
+		ktd253_backlight_set_max_ratio(ktd253);
 		current_ratio = KTD253_MAX_RATIO;
 	}
 
-	/*
-	 * WARNING:
-	 * The loop to set the correct current level is performed
-	 * with interrupts disabled as it is timing critical.
-	 * The maximum number of cycles of the loop is 32
-	 * so the time taken will be (T_LOW_NS + T_HIGH_NS + loop_time) * 32,
-	 */
-	local_irq_save(flags);
 	while (current_ratio != target_ratio) {
 		/*
 		 * These GPIO operations absolutely can NOT sleep so no
 		 * _cansleep suffixes, and no using GPIO expanders on
 		 * slow buses for this!
 		 */
-		gpiod_set_value(ktd253->gpiod, 0);
-		ndelay(KTD253_T_LOW_NS);
-		gpiod_set_value(ktd253->gpiod, 1);
-		ndelay(KTD253_T_HIGH_NS);
-		/* After 1/32 we loop back to 32/32 */
-		if (current_ratio == KTD253_MIN_RATIO)
+		ret = ktd253_backlight_stepdown(ktd253);
+		if (ret == -EAGAIN) {
+			/*
+			 * Something disturbed the backlight setting code when
+			 * running so we need to bring the PWM back to a known
+			 * state. This shouldn't happen too much.
+			 */
+			gpiod_set_value_cansleep(ktd253->gpiod, 0);
+			msleep(KTD253_T_OFF_MS);
+			ktd253_backlight_set_max_ratio(ktd253);
+			current_ratio = KTD253_MAX_RATIO;
+		} else if (current_ratio == KTD253_MIN_RATIO) {
+			/* After 1/32 we loop back to 32/32 */
 			current_ratio = KTD253_MAX_RATIO;
-		else
+		} else {
 			current_ratio--;
+		}
 	}
-	local_irq_restore(flags);
 	ktd253->ratio = current_ratio;
 
 	dev_dbg(ktd253->dev, "new ratio set to %d/32\n", target_ratio);