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arm64: dts: qcom: sc8180x-primus: Fix HALL_INT polarity

Message ID 20231130-sc8180x-primus-lid-polarity-v1-1-da917b59604b@quicinc.com
State Accepted
Commit 1aaa08e8de365cce59203541cafadb5053b1ec1a
Headers show
Series arm64: dts: qcom: sc8180x-primus: Fix HALL_INT polarity | expand

Commit Message

Bjorn Andersson Dec. 1, 2023, 12:11 a.m. UTC
The hall sensor interrupt on the Primus is active low, which means that
with the current configuration the device attempts to suspend when the
LID is open.

Fix the polarity of the HALL_INT GPIO to avoid this.

Fixes: 2ce38cc1e8fe ("arm64: dts: qcom: sc8180x: Introduce Primus")
Signed-off-by: Bjorn Andersson <quic_bjorande@quicinc.com>
---
 arch/arm64/boot/dts/qcom/sc8180x-primus.dts | 2 +-
 1 file changed, 1 insertion(+), 1 deletion(-)


---
base-commit: 3cd3fe06ff81cfb3a969acb12a56796cff5af23d
change-id: 20231130-sc8180x-primus-lid-polarity-54aa6405f61d

Best regards,
diff mbox series

Patch

diff --git a/arch/arm64/boot/dts/qcom/sc8180x-primus.dts b/arch/arm64/boot/dts/qcom/sc8180x-primus.dts
index fd2fab4895b3..a40ef23a2a4f 100644
--- a/arch/arm64/boot/dts/qcom/sc8180x-primus.dts
+++ b/arch/arm64/boot/dts/qcom/sc8180x-primus.dts
@@ -43,7 +43,7 @@  gpio-keys {
 		pinctrl-0 = <&hall_int_active_state>;
 
 		lid-switch {
-			gpios = <&tlmm 121 GPIO_ACTIVE_HIGH>;
+			gpios = <&tlmm 121 GPIO_ACTIVE_LOW>;
 			linux,input-type = <EV_SW>;
 			linux,code = <SW_LID>;
 			wakeup-source;